Skip to content
NOWCAST KCRA 3 News at 5am
Live Now
Advertisement

NTSB report finds Dali lost power day before crashing into Key Bridge in Baltimore

NTSB releases preliminary report on Dali collision with Key Bridge

NTSB report finds Dali lost power day before crashing into Key Bridge in Baltimore

NTSB releases preliminary report on Dali collision with Key Bridge

COMING UP IN A FEW MINUTES. TOMORROW THE NTSB WILL WILL TESTIFY BEFORE CONGRESS ON ITS RESPONSE TO THE KEY BRIDGE COLLAPSE. AND TONIGHT, THE AGENCY RELEASED ITS PRELIMINARY REPORT ON THE DISASTER. INVESTIGATORS LEARNED TEN HOURS BEFORE THE DOLLY CARGO SHIP LEFT BALTIMORE AND COLLIDED WITH THE BRIDGE. IT EXPERIENCE A BLACKOUT. A CREW MEMBER MISTAKES CLOSED AN ENGINE EXHAUST DAMPER. DOING SO CAUSED THE SHIP TO STALL. THE SHIP THEN EXPERIENCED A SECOND BLACKOUT THE MORNING OF MARCH 26TH. THAT HAPPENED BECAUSE THE BREAKERS OPENED UNEXPECTEDLY. AT THE TIME, THE DOLLY WAS JUST TWO MILES. EXCUSE ME, POINT TWO MILES FROM THE KEY BRIDGE. THE CREW DID MANAGE TO REGAIN THE ELECTRIC POWER BEFORE THE SHIP HIT THE BRIDGE. HOWEVER, THEY WERE NOT ABLE TO REGAIN PROPULSION, WHICH CAUSED THE SHIP TO THEN SLAM INTO THE STRUCTURE. AT THIS POINT, THE NTSB CANNOT SAY EXACTLY WHICH OF THESE ISSUES CAUSED THE SHIP TO HIT THE BRIDGE, AND IN ADDITION TO THE SIX CONSTRUCTION WORKERS WHO DIED, A MEMBER OF THE DOLLY CREW WAS ALSO INJURED WHEN THE BRIDGE FELL. MEANTIME, MARYLAND REACHED A BIG MILESTONE IN CLEANUP EFFORTS. OFFICIALS WITH UNIFIED COMMAND SAYING THAT THE OPERATION TO REMOVE A BRIDGE TRUSS FROM THE DOLLY WAS SUCCESSFUL. BUT THERE’S STILL PLENTY OF WORK TO BE DONE. 11 NEWS REPORTER KIM DACEY JOINS US LIVE FROM SPARROWS POINT WITH THE DETAILS. HEY, KIM. WELL, JASON, UNIFIED COMMAND DIDN’T WASTE ANY TIME GETTING BACK TO WORK AFTER THE DETONATION. THEY STARTED IMMEDIATELY WORKING THROUGH THE NIGHT AND EVEN THROUGH TODAY TO MAKE THEIR ASSESSMENT ABOUT WHERE THINGS LIE HERE, HERE, NOW, AFTER THE DETONATION. WHAT MIGHT HAVE SHIFTED AND HOW BEST TO MOVE FORWARD. AND WITH THAT, THE MOST DANGEROUS, COMPLICATED AND DRAMATIC PART OF THE KEY BRIDGE RECOVERY MISSION IS COMPLETE. IT WAS PLANNED. IT WAS METHODICAL. IT WAS SAFE. AND IMPORTANTLY, THERE WERE ZERO INJURIES. GOVERNOR WES MOORE TALKED TO T.J. SMITH ON WBAL NEWS RADIO TUESDAY MORNING. HE AND UNIFIED COMMAND SAY THE OPERATION WAS A SUCCESS. AS YOU SAW, IT WAS VERY LOCALIZED. IT REMAINED AROUND THE STEEL AND ON THE WRECKAGE. THE CUTS OCCURRED AS THEY WERE PLANNED. AND WHILE WE STILL HAVE SOME SPANS THAT REMAIN, SOME SOME STEEL THAT’S STILL SITTING ON THE DOLLY, WE ALWAYS WERE PLANNING ON REMOVING ANY WRECKAGE THAT WE NEEDED TO. THEY SAY THEY ALREADY HAVE CHASSIS, THE CRANE AND GUS THE GRABBER READY TO GO TO REMOVE THE WRECKAGE. AT THE SAME TIME, THEY’RE ASSESSING HOW THE DOLLY IS SITTING NOW, AND THE BEST WAY TO REFLOAT IT. THEN. THE PLAN IS TO USE TUGBOATS TO TAKE IT TO THE PIER AT SEAGIRT. THEY’RE GOING TO TAKE THE REMAINING ROADWAY THAT’S ON TOP OF THE DOLLY, AND SOME OF THE OTHER WRECKAGE ON THERE, AND REMOVE THAT. UM, THEN THEY’RE GOING TO REMOVE SOME CONTAINERS OVER THERE. UH, AND THEN THE PLAN WOULD BE FOR THEM TO DO SOME TYPE OF TEMPORARY REPAIRS. O’CONNELL SAYS THE DOLLY WILL REMAIN AT SEAGIRT FOR 4 TO 6 WEEKS UNTIL IT’S TAKEN DOWN TO NORFOLK FOR MORE EXTENSIVE REPAIRS. OFFICIALS SAY THIS IS A HUGE MILESTONE, BUT THERE IS STILL PLENTY OF WORK TO BE DONE TO GET THE MAIN SHIPPING CHANNEL BACK OPEN. WE’RE GOING TO BE MOVING TO THE FAR SIDE OF THE CHANNEL TO CONTINUE GETTING THAT DOWN ALL THE WAY TO 50FT. WE’RE VERY CLOSE AND THEN CONTINUING TO WIDEN IT WHEN WE GET TO 400FT WIDE, WE’RE GOING TO BE ABLE TO BRING ANYTHING, ANYTHING THAT NEEDS TO COME INTO THE PORT OF BALTIMORE. OFFICIALS AREN’T SURE EXACTLY HOW LONG IT WILL TAKE TO REFLOAT THE DOLLY, BUT THEY’RE HOPING TO DO THAT WITHIN THE NEXT COUPLE OF DAYS.
Advertisement
NTSB report finds Dali lost power day before crashing into Key Bridge in Baltimore

NTSB releases preliminary report on Dali collision with Key Bridge

The Dali container ship lost power twice the day before crashing into the Francis Scott Key Bridge, causing its collapse, according to a preliminary National Transportation Safety Board report released Tuesday afternoon. The NTSB's marine investigation preliminary report into the Dali revealed one of the 23 crew members was injured on board the ship when the bridge fell.| PDF: View the NTSB's full report hereThe U.S. Coast Guard classified this accident as a major marine casualty.NTSB: Dali experienced power outage day before crashThe report found the Dali experienced a power outage on March 25 during maintenance, about 10 hours before it departed Baltimore. "A crewmember mistakenly closed an inline engine exhaust damper."The NTSB report explains that the closure blocked the engine's cylinder exhaust gases from traveling up its stack and out of the vessel, causing the engine to stall."When the system detected a loss of power, generator No. 3 automatically started," the report states.NTSB: Second power outage reported on way to bridgeThe report also establishes a timeline on the morning of March 26 when a primary electrical breaker that feeds most of the Dali's equipment and lighting tripped, causing the ship to lose power and a blackout to occur.Then, the main propulsion diesel engine shut down automatically after pumps lost electrical power, so the ship lost main propulsion and its propeller stopped. The report found that the crew was able to restore electrical power, called for a tug assist and dropped an anchor.The report then found a second blackout occurred and a marine radio call was made to warn all waterborne traffic shortly before the Dali struck the bridge.Alcohol and drug testing of ship pilots and most of the crew came back negative, the report states.Test results of the three main grades of fuel for the main engine and electrical generators found no concerns related to the quality of the fuel. Additional fuel samples were taken from all fuel tanks, but no quality concerns were found.At this point, the NTSB could not say exactly which issue caused the ship to hit the bridge as the NTSB continues to investigate.NTSB leaders are scheduled to testify Wednesday before Congress on its response to the bridge collapse.

The Dali container ship lost power twice the day before crashing into the Francis Scott Key Bridge, causing its collapse, according to a preliminary National Transportation Safety Board report released Tuesday afternoon.

The NTSB's marine investigation preliminary report into the Dali revealed one of the 23 crew members was injured on board the ship when the bridge fell.

Advertisement

| PDF: View the NTSB's full report here

The U.S. Coast Guard classified this accident as a major marine casualty.

NTSB: Dali experienced power outage day before crash

The report found the Dali experienced a power outage on March 25 during maintenance, about 10 hours before it departed Baltimore. "A crewmember mistakenly closed an inline engine exhaust damper."

The NTSB report explains that the closure blocked the engine's cylinder exhaust gases from traveling up its stack and out of the vessel, causing the engine to stall.

"When the system detected a loss of power, generator No. 3 automatically started," the report states.

NTSB: Second power outage reported on way to bridge

The report also establishes a timeline on the morning of March 26 when a primary electrical breaker that feeds most of the Dali's equipment and lighting tripped, causing the ship to lose power and a blackout to occur.

Then, the main propulsion diesel engine shut down automatically after pumps lost electrical power, so the ship lost main propulsion and its propeller stopped. The report found that the crew was able to restore electrical power, called for a tug assist and dropped an anchor.

The report then found a second blackout occurred and a marine radio call was made to warn all waterborne traffic shortly before the Dali struck the bridge.

Alcohol and drug testing of ship pilots and most of the crew came back negative, the report states.

Test results of the three main grades of fuel for the main engine and electrical generators found no concerns related to the quality of the fuel. Additional fuel samples were taken from all fuel tanks, but no quality concerns were found.

At this point, the NTSB could not say exactly which issue caused the ship to hit the bridge as the NTSB continues to investigate.

NTSB leaders are scheduled to testify Wednesday before Congress on its response to the bridge collapse.